4GWGD4815FW1 Whirlpool Dryer - Instructions
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My dryer only heats up at the beginning of cycle so my clothes will not dry.
I remove the front control panel and to get to the bottom front dryer door off. Using my volt meter i checked all the sensors and thermal. I surf the internet for hint and some one mention to replace the coil since some time you could have one goes out and the other working still. After i replaced the coil kit it works like a champ.
Parts Used:
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Monique from Mission Viejo, CA
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Difficulty Level:A Bit Difficult
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Screw drivers, Socket set
31 of 39 people
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Dyer drum doesnt turn
It was really quite esy remove the screws from the back and pop the top off . then remove 2 top inside screws from the front , lift the front off the sides , support the drum and lift out , you will then see the idler wheels, replace them with the new ones ,replce the tensioner , wrap the belt around the drum, need help putting the drum back in the case, have someone hold the drum in place while you lay on the ground and put the belt around the motor pulley and the tensioner on the bottom.you then put the front panel back into place and secure with the 2 inside screws, then put the rest back together in reverse oder. ... hope this helps someone
Parts Used:
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Shawn from Akron, OH
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Pliers, Screw drivers
27 of 29 people
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no heat
the ignitor did not glow red checked thermal fuse by exhaust duct. fuse open replaced thermal fuse
Parts Used:
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rex from streator, IL
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Wrench (Adjustable)
30 of 39 people
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Dryer would dry for 5-10 minuets then no heat
I tested the dryer coils and found that they were getting a voltage but would not open the gas valve. Coils were not bad but weak. After they warmed up they would not open the gas valve. It took 10 min to repace both coils and the heat sensor.
Parts Used:
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Richard from Jerome, MI
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Difficulty Level:Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers, Socket set
35 of 55 people
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Drayer Was Making Squeaking Sound
Took off the top and front panel. Found that the belt tensioner was worn out. Decided to pull drum out,and replace the belt and drum rollers also. Put it back together, and it works fine.
Parts Used:
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Charles from Gray, TN
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Pliers, Screw drivers
26 of 30 people
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Dryer would not heat up.
I unplugged the dryer,removed the two small screws on the front of the dryer and pulled the bottom forward. The two wires connected to the door do not have to be removed. With an electrical tester using the Ohm setting I tested the Radiant sensor and the Gas Valve coils. The two terminal coil was DOA. The dryer can be operated with the front open as long as the door wires are connected. Symptons: The igniter would heat up and not release gas. My repair was successfull due to this awesome website and the super fast shipping service. AAAA++++
Parts Used:
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Roger from Bonners Ferry, ID
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Nutdriver, Screw drivers
26 of 30 people
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Dryer would not tumble.
I wasn't sure if the problem was the belt (probable) or the idler pulley assembly (less likely) but the total for both parts was about $26 plus shipping. So why not replace both to be sure?
As it turns out, my original idler pulley assembly does not turn. Rather, it has a concave semi-circular piece that is fixed in place. The belt ran in a groove in that piece.
The replacement part has a nylon wheel that turns. As a result of replacing the idler pulley assembly (which I don't think was necessary to fix my tumbling problem) the dryer runs much quieter. (We used to get a fair amount of squeaking when the belt rubbed).
As for the actual repair (I would rate myself as above average on tackling household repairs), it was about the simplest repair I've ever done. I followed the video provided on this site (excellent video) and it took less than 20 minutes -- cleaning up all of the lint/odds and ends under the washer and dryer took longer than the actual repair.
My only issue (minor) was disconnecting the electric harness. It did not slide as easily as in the video. I had to coax mine a bit with a small screwdriver (make sure your dryer is unplugged!!). I suspect it was simply a function of the harness never being unplugged -- the dryer is 9 years old.
I also felt great because I'm sure I saved a $125 service call (for only $26 in parts and 20 minutes of my life).
Good luck!
As it turns out, my original idler pulley assembly does not turn. Rather, it has a concave semi-circular piece that is fixed in place. The belt ran in a groove in that piece.
The replacement part has a nylon wheel that turns. As a result of replacing the idler pulley assembly (which I don't think was necessary to fix my tumbling problem) the dryer runs much quieter. (We used to get a fair amount of squeaking when the belt rubbed).
As for the actual repair (I would rate myself as above average on tackling household repairs), it was about the simplest repair I've ever done. I followed the video provided on this site (excellent video) and it took less than 20 minutes -- cleaning up all of the lint/odds and ends under the washer and dryer took longer than the actual repair.
My only issue (minor) was disconnecting the electric harness. It did not slide as easily as in the video. I had to coax mine a bit with a small screwdriver (make sure your dryer is unplugged!!). I suspect it was simply a function of the harness never being unplugged -- the dryer is 9 years old.
I also felt great because I'm sure I saved a $125 service call (for only $26 in parts and 20 minutes of my life).
Good luck!
Parts Used:
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John from Minneapolis, MN
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Screw drivers
24 of 25 people
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Convert gas dryer to Propane
Received conversion kit. Removed front dryer panel,2 screws. Removed burner tube, 2 screws then removed natural gas orfice.
Installed propane orfice and repalced burner tube.
Removed regulater plug and replaced with new plug from kit using 90 degree ratchet screw driver. Approximately 20 minutes. Dryer working great.
Installed propane orfice and repalced burner tube.
Removed regulater plug and replaced with new plug from kit using 90 degree ratchet screw driver. Approximately 20 minutes. Dryer working great.
Parts Used:
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Leonard from Lemitar, NM
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Socket set
25 of 30 people
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noisy drum
the job would have gone faster if the right parts had been sent in the first place. I would have never paid for two day shipping. In the repair, I removed the rear panel, clipped the plastic triangle holding the bearing, installed the new bearing and new clip.
Parts Used:
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Jeff from Mesa, AZ
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Difficulty Level:A Bit Difficult
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Screw drivers, Wrench (Adjustable), Wrench set
27 of 37 people
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dryer stoped heating
the problem was not the igniter its was the thermal fuse I broke the igniter during inspection of the problem be careful its a very easy thing to break repairs complete thank you parts select for the quick shipping and low prices
Parts Used:
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valerie from Elasmore, KS
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver
23 of 26 people
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Dyer would not heat, flame would shut off within 10 seconds
I opened the panel, undid the plugs, detached the radiant sensor by undoing one screw and removed and replaced the part. Fairly simply.
Parts Used:
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Christy from Riley, MI
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Difficulty Level:Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers, Socket set
24 of 29 people
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The dryer belt broke. During the effort to replace the belt it was noted that the lint trap housing seals were in need of replacement.
With the dryer taken apart to replace the broken belt it was obvious that the lint seals had not been working properly due to the excessive amount of lint covering all of the inside surfaces of the dryer. The belt idler pully had also moved from its normal mounting position and was laying at the bottom of the dryer. Because the lint had covered the bottom before the belt broke it was obvious to determine where the idler pully attached to the bottom.
Before cleaning I marked the exact location where the idler pully mounted to the bottom of the dryer.
While waiting for the replacement parts to be delivered a vacuum cleaner was used to remove lint from the inside surfaces of the dryer as well as the old fragments of the lint trap housing seals were removed and surfaces where the new seals would attach were cleaned.
Assembling the dryer with the new belt was a challenge due to the lack of support for the drum while getting the new belt in place, lined up properly, threaded through the idler pully and attached to the motor drive shaft. This is how I installed the new belt:
I used a piece of wood wider than the sides of the dryer, drilled holes that allowed for a piece of cloths line rope to be looped through and used to support the door opening end of the drum.
The drum was set on the seal and rollers at the back of the dryer.
The temporary wood /rope hanger was placed at the front end of the dryer resting on the sides with the top of the dryer raised.
The rope was adjusted until the drum rested on the back rollers and the rope like it would be positioned normally.
The new belt was then gently installed under the temporary support rope and around the drum.
The new belt had many kinks from shipping and was difficult to align with the location on the drum where it needs to ride so small strips of tape were temporarily used to hold the new belt in position until it could be fed through the idler pully and on to the drive shaft.
Several small pieces of a cardboard box were used to shim under the idler pully to hold it in its proper location as well as to make the belt attachment to the drive shaft easier.
With the belt attached, the temporary cardboard shims were removed from under the idler pully.
The front of the dryer was attached .
The temporary board and rope hanger was removed.
The tape that had been placed over the new belt to hold it in proper alignment was removed as the drum was rotated slowly by hand to ensure that all tape was removed prior to closing the top of the dryer.
The seals as well as the remainder of the dryer assembly was completed without any problems.
The dryer ran well for its initial trial spin and has dried several loads of laundry since.
Great parts and support Thankyou
Before cleaning I marked the exact location where the idler pully mounted to the bottom of the dryer.
While waiting for the replacement parts to be delivered a vacuum cleaner was used to remove lint from the inside surfaces of the dryer as well as the old fragments of the lint trap housing seals were removed and surfaces where the new seals would attach were cleaned.
Assembling the dryer with the new belt was a challenge due to the lack of support for the drum while getting the new belt in place, lined up properly, threaded through the idler pully and attached to the motor drive shaft. This is how I installed the new belt:
I used a piece of wood wider than the sides of the dryer, drilled holes that allowed for a piece of cloths line rope to be looped through and used to support the door opening end of the drum.
The drum was set on the seal and rollers at the back of the dryer.
The temporary wood /rope hanger was placed at the front end of the dryer resting on the sides with the top of the dryer raised.
The rope was adjusted until the drum rested on the back rollers and the rope like it would be positioned normally.
The new belt was then gently installed under the temporary support rope and around the drum.
The new belt had many kinks from shipping and was difficult to align with the location on the drum where it needs to ride so small strips of tape were temporarily used to hold the new belt in position until it could be fed through the idler pully and on to the drive shaft.
Several small pieces of a cardboard box were used to shim under the idler pully to hold it in its proper location as well as to make the belt attachment to the drive shaft easier.
With the belt attached, the temporary cardboard shims were removed from under the idler pully.
The front of the dryer was attached .
The temporary board and rope hanger was removed.
The tape that had been placed over the new belt to hold it in proper alignment was removed as the drum was rotated slowly by hand to ensure that all tape was removed prior to closing the top of the dryer.
The seals as well as the remainder of the dryer assembly was completed without any problems.
The dryer ran well for its initial trial spin and has dried several loads of laundry since.
Great parts and support Thankyou
Parts Used:
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Benjamin from WELLS, ME
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Difficulty Level:A Bit Difficult
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver
23 of 26 people
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Scratches in Surface
This product comes in a bottle with a brush like Liquid Paper. It goes on incredibly easy. A second coat might be needed. I wanted to prevent rust from setting in so I covered the scratches and dings. The paint is a little brighter since my washer is 10 years old but it still looks great.
Parts Used:
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Michelle from Richardson, TX
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
75 of 183 people
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A high pitched squeal when drum was rolling.
First my son and I moved the dryer to the garage as we believed there would be a lot of lint possible during disassembly. Used a flat head screwdriver to pop the top from dryer housing. Then removing 2 nuts to facilitate the removal of the front of the dryer. The drum was able to be removed to diagnose the offending drum roller wheel. The drum roller wheel has experienced a failure as it had melted off of the metal spacer. Removing it and replacing with the new one was pretty easy. We then used a shop vac and an air hose to clean out all the lint, coins, paper clips and lost jewelry. Surprisingly there was not a single sock in there. Put it all back together in reverse order and plugged it in and now spins like a dream.
Parts Used:
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Robert from GOODRICH, TX
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Pliers, Screw drivers, Socket set
22 of 24 people
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Belt broke, dryer stopped.
Replaced the belt and the wheels supplied with the kit. I also cleaned the inside of the unit. It looks and works like new.
Parts Used:
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Richard from Groveland, MA
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Difficulty Level:Easy
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Total Repair Time:Less than 15 mins
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Tools:Nutdriver, Screw drivers
24 of 30 people
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